4d6c6c109b94d494376b594709559506abab2b07
Clear-noon peak (2026-06-24 13:44, HA recorder): each inverter ~4.7kW @ ~300V @ ~16A. A down string reads ~10A; ~16A = both parallel strings live. The "one string down per inverter" belief was from confounded afternoon/rainy samples + transient pv_loss_warning (now off) and is refuted. ~66% of nameplate at peak is explained by 45-deg tilt (wrong for high June sun), heat derate, and tree shading. AND the peak was demand-limited: battery charge pinned at the 120A cap (121A) at 65% SoC with only 3.3kW load -- reversing the earlier off-peak "not clipping" note. Documented the throttle test to resolve true array ceiling before raising max_charging_current. Co-Authored-By: Claude Opus 4.8 (1M context) <noreply@anthropic.com>
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